Ok, WOW I got lucky! So on my way home from the best job a man could ever have (haaah!) I ran into a real bad traffic jam. I decided to double back and hit the autoparts store up for a vacuum guage. Got it. Then, I got home, and my sickly girlfriend gave me a by, so I took full advantage. Backed the valves off one full turn, and it ran like a paraplegic. But it ran just enough that I could run around to the engine and loosen all valves... odd part is that I backed the valves 8* (1/4) turns (2 full turns) until they clacked and shut her down. She still runs PHEW!!! I'm going to have to get back at it tomorrow or as soon as I get a chance... I've got my brothers Sportster stripped down to the frame so we can chop it and put a hard tail on it F* YEAH! We might do that this weekend. Anyway. here's my thoughts.
-Rockers were already way too tight... as far as my math goes, they were 3/4 turn tighter than they should have been.
-If they were this tight... and drove for a long time... I'm guessing the damage is done... Because,...
-I put a piece of paper up to both sides of the exhaust tonight, and the starboard exhaust was hotter and it seemed to flutter more. I noticed this as a fact prior to my valve adjustment... So if anything... and I don't believe, but I may have exacerbated the issue.
-It may be a burnt exhaust valve on at least cylinder 8 likely 6 too at least.
-I'll redo the valve adjustment asap since I don't think the truck was warmed up significantly when I did it tonight, I'll fix the vacuum leak(s) and report back asap.
Oh, and I did notice a fishy looking whitish "tracking" mark on one of my spark plug wire boots... I noticed this when I was putting the wires back on the distributor, and don't know which orientation I had the wires before. I will keep my peeper peeled for this too.
-Rockers were already way too tight... as far as my math goes, they were 3/4 turn tighter than they should have been.
-If they were this tight... and drove for a long time... I'm guessing the damage is done... Because,...
-I put a piece of paper up to both sides of the exhaust tonight, and the starboard exhaust was hotter and it seemed to flutter more. I noticed this as a fact prior to my valve adjustment... So if anything... and I don't believe, but I may have exacerbated the issue.
-It may be a burnt exhaust valve on at least cylinder 8 likely 6 too at least.
-I'll redo the valve adjustment asap since I don't think the truck was warmed up significantly when I did it tonight, I'll fix the vacuum leak(s) and report back asap.
Oh, and I did notice a fishy looking whitish "tracking" mark on one of my spark plug wire boots... I noticed this when I was putting the wires back on the distributor, and don't know which orientation I had the wires before. I will keep my peeper peeled for this too.